CASE STUDY: DUVERNAY WAX
Pulling 158% more oil out of the ground in Central Alberta
The operator was having issues with two free-flowing wells. The first well was completely waxed off with nearly no flow, the second flowing inconsistently.
After benchmarking tests with our Para-Solvent, ReNuu pumped 20 liters of Para-Solvent and 100 liters of micro-organisms down the tubing with the wells shut-in, at a minimal cost. One well was restarted 2 hours later, cleared things up. The well had no trouble lifting condy. The second began flowing shortly after. This project had a significant positive ROI for the client, whom we continue to partner with moving forward.
258% production for under $600.
As the pictures indicate, the operator immediately saw increased gas production, as well as more consistent flow and pressures. Production jumped from 8-9 decks per day to 22!